Question
L6470: Several problems evaluating a Stepper-Motor Application
Posted on November 09, 2012 at 03:39
Hello,
We are currently evaluating the L6470 to drive analytic high-pressure pumps for Mass spectrometry.The final goal is to drive a stepper-motor in high precision micro-stepping mode at around 1.7 Nm at a maximum Speed of around 100 rpm.For evaluation we used a small bipolar stepper-motor from a previous test with the following parameters:- Model: Trinamic QSH4218-51-10-049 (Short Specs attached)
- Rated Phase Current: 1 A
- Phase Current: 5 ?
- Phase Inductance: 8 mH
- Measured K_e: 0.02041 (attached file: BMF Parameters)
As motor driver we used the EVAL6470H board attached to a STEVAL-PCC009V1 USB-SPI Interface in combination with the dSPIN Evaluation Tool 1.7.
Further Parameters:- Supply Voltage: 30 V
- The Motor accelerated at different rates (we tested 2000, 1000, 500, 100 Steps/s�) to different speeds. We tried to get it to as high as about 2000 Steps/s but it always stalled without any external force at about 1500 Steps/s (1/128 micro-stepping).
- The ''Command Error'' Flag very often was set after setting parameters with the Evaluation Tool.
Here our Questions:
- What could be the reasons the motor stalls at this stepprate and how could we avoid it in a ''real world'' application?
- Why was the ''Command Error'' set? Is there any possibility of diagnosis? (Cables where really short, the one that was shipped with the STEVAL-PCC009V1, about 10 cm)
We really looking forward for your answers and thank you for your efforts in advance!
Sincerely yours #stepper-motor-driver #stepper-motor #l6470